Author Topic: 572  (Read 195655 times)

M4wdFab

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Re: 572
« Reply #930 on: April 23, 2014, 07:38:30 AM »
so i finish my 10 minutes of packing and mount 2 new trailer tires, go to pull buggy out of shop, running and stumbling like crap and while im looking for a coil wire or cracked plug or some sensor loose i notice there is coolant pouring from the front of the block around the water pump.  awesome.   Pull the pump and find the compression limiting gasket is nuked.  run to shitbox store and get 2 new gaskets, and an entire water pump assembly that also comes with its gaskets.

decided the welder is buried and packed so sealing up the new WP heater outlets will be a hassle.  Throw new gaskets at old pump with everything cleaned up.  what a PITA to line up these gaskets without the bolts falling out.  start car, fill coolant system, and still has small drip in same place but not pouring out like before.  motor starts making horrendous high pitch screeching sound with 4psi oil less than normal now.  after 20 min of searching, the hose i rerouted ( i think PCV from left head) into the manifold that was causing my throttle to stick on is now causing all the noise in the intake, the motor running like shit, and the oil pressure.  i have no idea, that hose is hanging now and the manifold port plugged.  ignoring the coolant drip for now.

had not planned on a late night.

JEEPWERX

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Re: 572
« Reply #931 on: April 23, 2014, 08:21:19 AM »
WTF brutality the night before departure.

M4wdFab

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Re: 572
« Reply #932 on: April 24, 2014, 01:56:22 PM »
Two fan issues and a burnt coil wire for the wreck wheel win!

mr.mindless

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Re: 572
« Reply #933 on: April 24, 2014, 03:03:54 PM »
bad PCV valve on that hose letting raw vacuum into the valve cover and everything inside very angry about that? only thing that can make sense....
Quote from: etk300ex
oh lord!

KingtheZJ

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Re: 572
« Reply #934 on: April 28, 2014, 04:32:22 PM »
« Last Edit: April 28, 2014, 04:40:41 PM by KingtheZJ »

M4wdFab

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Re: 572
« Reply #935 on: April 28, 2014, 04:47:16 PM »
they make a 9/16" with a 3/4" socket which is what we use with the thick alum bead locks there is no room.  i thought ford 60's use 1/2" thread sometimes so check that


M4wdFab

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Re: 572
« Reply #937 on: May 01, 2014, 10:27:57 AM »
quick Bath tonight
Replace a fan
Check out seat
mount up the Boggers

M4wdFab

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Re: 572
« Reply #938 on: May 02, 2014, 09:18:41 AM »
 8)

GBR928

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Re: 572
« Reply #939 on: May 02, 2014, 09:43:15 AM »
Did the van you got the engine out of have hydroboost?


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M4wdFab

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Re: 572
« Reply #940 on: May 02, 2014, 10:30:24 AM »
good question- i dont recall.  it was a 2004 2500 express van, 6 lug

There is a factory power brake fitting plug that would be installed in the manifold we could check on 571 and 572.  571's motor was unknown application also. 


I recall ryans 6.0 motor did have hydroboost and had the plug we had to remove. 

matt

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Re: 572
« Reply #941 on: May 02, 2014, 12:12:27 PM »
that looks pretty sinister with the boggers on it......

M4wdFab

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Re: 572
« Reply #942 on: May 02, 2014, 01:02:22 PM »
def looks like it has anger issues up close.  hard to get a good picture.  its like 96" wide

M4wdFab

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Re: 572
« Reply #943 on: May 06, 2014, 10:30:13 AM »
got a power wash bath
full bolt check
heims lubed
front shaft pulled and HD tubed
gage splash guard installed
lower king pins new grease fittings
grease pumped in many places

M4wdFab

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Re: 572
« Reply #944 on: May 08, 2014, 10:58:42 AM »
ups express 18 hrs came through!