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Green monster

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M:
you were driving it?

M4wdFab:
lol, Math i assume not driving



you are brave to consider.

mr.mindless:
Math, not driving. 330hp probably wouldn’t push the brick that fast.

It is not currently a runner. It’s shut down with some sort of computer problem, and has been parked ever cents. A Cummins technician got a running to move it to the spot that it’s in right now. I did not see any obvious electrical jumpers around the ECM. I’ve done a lot of reading and I found a very small handful of possible causes, none of which are terribly frightening.

With the Jack hydraulic leak, I was not able to lift the cab to look over wiring more thoroughly. For some reason, I was also unable to use my jump box to get adequate voltage for key – on self tests or reading codes. For some reason, my jump box thought that polarity was reversed when I used the jump terminal. Without being able to till the cab, I cannot get to the actual battery terminals. ECM fuses should be directly off the battery so I was also unable to verify their condition.


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mr.mindless:
build sheet

mr.mindless:
engine dataplate

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